Originally Posted by
Failure
Who might i ask was tuning this.
It wasn't an issue with the tune...I whole heartedly trust the man who did the tuning on the car.
The failure (at least with the piston) was a result of the sump pump set up on the fuel system. The sadle design of the tank on the X most likely resulted in fuel being slosed away from the pump (only about an 1/8 of a tank of sunoco 117 in the car at the time). The momentary lack of fuel at 8500rpm's is what more than likely caused the problem.
I'm a bit dumb on the issue but that is how it was explained to me.