matt
the TEC II took a shit on the dyno. we thought it was a failed crank sensor, turned out the whole tec II wasnt working. Swapped it out with the one in my daily car it fired up.
but now there is a strange issue with boost. it fluctuates from 12-14psi really slowly during a third gear pull. power is WAYYYYYY down at 279 @12psi at redline. fuel is a mix of 93 and 5 gallons of 116.
its either a wg problem or a fucked up exhaust manifold. meaning flow is all wrong
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$#@% a mandrel bend. JDM WELD IT!
VA resident invading your boards....wassup to my florida peeps.